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Hollow Rotary Actuator's Electronic Gear Follow Response is Out of Synchronization

Delila

New Member
Seeking Advice.

When debugging a hollow rotary actuator(OYOSTEPPER) in CNC electronic gear follow mode, it acts as the driven axis following the spindle in linkage.

Unloaded, the angle follow ratio is precise and error-free. However, under actual tooling load, the driven rotating end always exhibits a slight lag, with subtle deformation of the synchronization trajectory, affecting workpiece alignment accuracy.

I've recalculated the transmission ratio, tuned the servo closed-loop gain, and optimized the CNC synchronization timing, but the lag persists.

I suspect the actuator's dynamic response speed cannot keep up with the intelligent follow-up rhythm. Seeking advice from experienced experts on parameter tuning.
 

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